All,
An update on the '78E with '80 carbs situation: I think I've almost got it. So the current setup is the gentler 5IZ7 needles with 120 mains, I went down to #40 pilots, and am finally getting a decent color on the plugs, pending more testing. The last remaining issue was cyl #4 kept getting a sooty plug. I checked and rechecked everything, tested the choke circuit for leakage, etc. The rest of the carbs had the idle mixture screws set out to 3 turns out with the #40 pilots but #4 would get sooty even with just .75 turns out. Finally I pulled the mixture screws from cylinders 3 and 4 to compare, and did some flow testing with WD40 through the idle circuits and saw that #4 was flowing more past the idle mixture screw even though it was turned in tighter! Upon disassembly of #3 and #4 idle mixture screws I found that the o-rings are all pretty compressed into a tapered conical shape (the seat that they are pressed against). Well it seems that at some point when messing around I had reversed the direction of the o-ring on #4, and somehow(?) that was causing problems. Or maybe my "flow testing" fixed something. I don't know. But I swapped the idle mixture screws on 3 and 4 and the rich condition on #4 seems to have been resolved. The bike has the cleanest idle it's ever had, I've never been able to lug it down to 2000rpm like this before. I'll be fine tuning the idle mixture screws a bit more, I think I'm a tad lean at the moment (set them to 2.5 turns out). I'm also considering repacking the RC pipe with some looser type fiberglass wrap to help it flow a bit better (hopefully without getting too loud).
An update on the '78E with '80 carbs situation: I think I've almost got it. So the current setup is the gentler 5IZ7 needles with 120 mains, I went down to #40 pilots, and am finally getting a decent color on the plugs, pending more testing. The last remaining issue was cyl #4 kept getting a sooty plug. I checked and rechecked everything, tested the choke circuit for leakage, etc. The rest of the carbs had the idle mixture screws set out to 3 turns out with the #40 pilots but #4 would get sooty even with just .75 turns out. Finally I pulled the mixture screws from cylinders 3 and 4 to compare, and did some flow testing with WD40 through the idle circuits and saw that #4 was flowing more past the idle mixture screw even though it was turned in tighter! Upon disassembly of #3 and #4 idle mixture screws I found that the o-rings are all pretty compressed into a tapered conical shape (the seat that they are pressed against). Well it seems that at some point when messing around I had reversed the direction of the o-ring on #4, and somehow(?) that was causing problems. Or maybe my "flow testing" fixed something. I don't know. But I swapped the idle mixture screws on 3 and 4 and the rich condition on #4 seems to have been resolved. The bike has the cleanest idle it's ever had, I've never been able to lug it down to 2000rpm like this before. I'll be fine tuning the idle mixture screws a bit more, I think I'm a tad lean at the moment (set them to 2.5 turns out). I'm also considering repacking the RC pipe with some looser type fiberglass wrap to help it flow a bit better (hopefully without getting too loud).
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