Hi folks, I'm new to posting on this site, but I'd like to share some of my experiences with my xj1100 "Mad Maxine" project bike. My dad purchased it when I was in high school knowing it had the notorious 2nd gear issue. My older brother attempted to diagnose the problem with no luck and left a pile of parts and bolts when he abandoned it. A few years later, after I graduated, I decided to take on the issue myself and attempt a top end rebuild. I bought a manual and started reading this forum for ideas. I quickly learned that this was no small task. Back then, I had never worked on a four stroke, so this was my learning experience. I was also still an impatient teenager so I made lots of mistakes throughout the original project. I must have tore into the engine at least 5 times in order to finally get a running specimen over a 7 month period. Once I got it on three road for the first time I experienced the comfort of the low set seat along with the white knuckle thrust running through the shaft. It was the greatest 7 miles on a road bike that I had experienced up to that point. It was then, at 7 miles, that a valve dropped into the number 4 cylinder and got hammer into the head by the piston. All of that time and money I had put into it felt like a waist! I parked the bike and moved on to other bikes and interests.
Fast forward 9 years to last year. At this point, I was now out of college and in a house with room to work. I decided to resurrect my juvenile passion and attempt to revive Maxine from her fallen state. I ordered a new top end, (head, cylinder, and piston) and took my time to rebuild it properly. I followed every step in the manual from pistons to valves to timing and even added some black engine paint to the top end for a clean look. I also meticulously wend through the carbs to ensure that every orifice was clean and clear. After assembly I learned that I had no spark. I spent hours sorting through the wiring diagrams to chase down the electrical gremlins that had snuck in over the 9 years of sitting. I finally found a broken wire near the shifter going into the left side case. I soldered it back together and punched the start button. The moment I had been waiting 9 years for had arrived as I experienced the low roar of the big in line 4. After some tuning. I had a decent running bike, accept for an occasional skipping first gear. I put about 200 miles on it with short rides around town. The ride was just as I remembered it 9 years earlier, smooth, comfortable, and fast! I got an opportunity one Saturday night last September to go for a ride with a buddy. We made it about 15 miles down the highway when I all of the sudden hear a loud knocking followed quickly by the engine locking up. I rolled to a stop and my buddy told me I had dumped oil all over the road. When we got it back to my place, I noticed a 2" Dia hole in the front of the case.
Again, I parked it until it warmed up enough for me to really look into it. I started into it this April after I found a replacement case with crank on ebay for a good price. After I removed the engine and tore it down, I discovered that the connecting rod on #3 and come unbolted. The results were the crank slapping the connecting rod through the front and back of the case also breaking chunks out of the sleeve and piston. All in all, not too bad.
I then proceeded with the task of transferring everything over to the new case. In the process, I also decided to perform the DreMel fix to my skipping gears. Since i had the old set of cylinders from 10 years ago lying around, i also took the good sleeves out to replace my broken one with. The BBQ grill made quick work of that! After a few weeks of work on it between career and family, I am almost ready to install the motor back in the bike. I have painted the case black to match the top end and polished the covers to give the two-tone look. I will post pictures as soon as I find out how! I still need to install the top end, but I'm not sure if I should do it inside or out of the frame. Any suggestions? Long story short, I'm excited for round 3 on this beast, and I hope that are no more catastrophic failures!
Fast forward 9 years to last year. At this point, I was now out of college and in a house with room to work. I decided to resurrect my juvenile passion and attempt to revive Maxine from her fallen state. I ordered a new top end, (head, cylinder, and piston) and took my time to rebuild it properly. I followed every step in the manual from pistons to valves to timing and even added some black engine paint to the top end for a clean look. I also meticulously wend through the carbs to ensure that every orifice was clean and clear. After assembly I learned that I had no spark. I spent hours sorting through the wiring diagrams to chase down the electrical gremlins that had snuck in over the 9 years of sitting. I finally found a broken wire near the shifter going into the left side case. I soldered it back together and punched the start button. The moment I had been waiting 9 years for had arrived as I experienced the low roar of the big in line 4. After some tuning. I had a decent running bike, accept for an occasional skipping first gear. I put about 200 miles on it with short rides around town. The ride was just as I remembered it 9 years earlier, smooth, comfortable, and fast! I got an opportunity one Saturday night last September to go for a ride with a buddy. We made it about 15 miles down the highway when I all of the sudden hear a loud knocking followed quickly by the engine locking up. I rolled to a stop and my buddy told me I had dumped oil all over the road. When we got it back to my place, I noticed a 2" Dia hole in the front of the case.
Again, I parked it until it warmed up enough for me to really look into it. I started into it this April after I found a replacement case with crank on ebay for a good price. After I removed the engine and tore it down, I discovered that the connecting rod on #3 and come unbolted. The results were the crank slapping the connecting rod through the front and back of the case also breaking chunks out of the sleeve and piston. All in all, not too bad.
I then proceeded with the task of transferring everything over to the new case. In the process, I also decided to perform the DreMel fix to my skipping gears. Since i had the old set of cylinders from 10 years ago lying around, i also took the good sleeves out to replace my broken one with. The BBQ grill made quick work of that! After a few weeks of work on it between career and family, I am almost ready to install the motor back in the bike. I have painted the case black to match the top end and polished the covers to give the two-tone look. I will post pictures as soon as I find out how! I still need to install the top end, but I'm not sure if I should do it inside or out of the frame. Any suggestions? Long story short, I'm excited for round 3 on this beast, and I hope that are no more catastrophic failures!
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