Brief recap. Bike revs too high - around 2500 to 3000 when hot. After searching earlier posts for the root of my problem I am starting to wonder if the float heights are off enough to cause this. When I cleaned the carbs I used a caliper and reset the float height at 25.7mm, which I believe is stock. I measured both sides and twisted the floats enough so that both sides appeared dead on.
Question: do these bikes run better when the float height is other than stock? Did I read the specs wrong and set the float height incorrectly?
When I first start the bike on full choke it idles well at frst, then the rev starts to climb as the bike warms up. When it starts revving high I put it on half choke and it goes back to a good idle for a while, then starts to climb again. When I take the choke off completely the idle is fine until the bike warms up completely and the idle revs high again.
This could still be a synch issue, but I'm skeptical. When cleaned the carbs I bench synched them. I then synched them with vacuum gauges when the carbs were mounted. They were very close from the bench synch and dialing them in required only a quarter turn or less on any of the adjusters.
I've sprayed WD40 around all of the intake manifolds looking for a leak and got no reaction.
I'm getting frustrated. Ideas welcome.
Patrick
Question: do these bikes run better when the float height is other than stock? Did I read the specs wrong and set the float height incorrectly?
When I first start the bike on full choke it idles well at frst, then the rev starts to climb as the bike warms up. When it starts revving high I put it on half choke and it goes back to a good idle for a while, then starts to climb again. When I take the choke off completely the idle is fine until the bike warms up completely and the idle revs high again.
This could still be a synch issue, but I'm skeptical. When cleaned the carbs I bench synched them. I then synched them with vacuum gauges when the carbs were mounted. They were very close from the bench synch and dialing them in required only a quarter turn or less on any of the adjusters.
I've sprayed WD40 around all of the intake manifolds looking for a leak and got no reaction.
I'm getting frustrated. Ideas welcome.
Patrick
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