Exactly what I thought...(and was afraid of)
Pulled the carbs over the weekend to see what's up. A whole can of worms, and then some!
Float levels : 25mm, 19mm(!!), 24mm, 21mm - Explains the wet no 2 and 4. Set all to 25mm.
Main jets - 137.5 (Plastic!) in 1,2,4 (Std for 79F per tech tips?) and 122.5(metal) in 3 !!!!!!!! Why you ask? Idle mixture screw in 3 broken off and 4 bent and in bad shape. (Also turned in too tight)
Bit of a bugger, as I can't seem to get it out, even with the push-pin trick.{ Yeah, this time I did my homework }The other problem : No-one in SA seems to stock these, unless I buy a complete carb kit (K+L)which comes to about $30 ea - Crazy!
Mate of mine is gonna look for some, also ordered some 140 or 142.5's (or closest that's available) mains from him (under $2 a piece) because of 4 in 1 and K&N.
Couldn't get no. 2 or 3 pilot jet out, as the groove is worn off (Idiot PO!) but sprayed it some penetrating oil and will try again tommorow, but everything was supprisingly clean.
Also, got the electrical gremlins sorted out. My own fault though...
Pinched a wire in the lights switch when I put it back, as one guru suggested. At least I now have a new, pretty looking fuse block, and wiring A-OK. Even the gas guage is working, wasn't before due to a loose earth connecter!
Getting there... slowly but surely!
More l8er
1H
Pulled the carbs over the weekend to see what's up. A whole can of worms, and then some!
Float levels : 25mm, 19mm(!!), 24mm, 21mm - Explains the wet no 2 and 4. Set all to 25mm.
Main jets - 137.5 (Plastic!) in 1,2,4 (Std for 79F per tech tips?) and 122.5(metal) in 3 !!!!!!!! Why you ask? Idle mixture screw in 3 broken off and 4 bent and in bad shape. (Also turned in too tight)
Bit of a bugger, as I can't seem to get it out, even with the push-pin trick.{ Yeah, this time I did my homework }The other problem : No-one in SA seems to stock these, unless I buy a complete carb kit (K+L)which comes to about $30 ea - Crazy!
Mate of mine is gonna look for some, also ordered some 140 or 142.5's (or closest that's available) mains from him (under $2 a piece) because of 4 in 1 and K&N.
Couldn't get no. 2 or 3 pilot jet out, as the groove is worn off (Idiot PO!) but sprayed it some penetrating oil and will try again tommorow, but everything was supprisingly clean.
Also, got the electrical gremlins sorted out. My own fault though...
Pinched a wire in the lights switch when I put it back, as one guru suggested. At least I now have a new, pretty looking fuse block, and wiring A-OK. Even the gas guage is working, wasn't before due to a loose earth connecter!
Getting there... slowly but surely!
More l8er
1H
Comment