Brief history
The bike had been running reasonably well but seemed to lack pulling power in the mid throttle range and had a misfire at constant throttle settings and a rough misfire idle. Mostly when warming up.
Last Thursday (July 27) I removed the baffle of my MAC 4 into 1 pipe and packed the outside of the baffle to control noise and possible poor exhaust resonance because the stop plate has been removed from the baffle. I used the bike the balance of that day for a few short trips. there was no change to the above condition it was just less noisy.
I parked the bike that Thursday evening to remove and return the front wheel for a defective tire issue.
Got the tire issue issue sorted and reinstalled on Wednesday (Aug 2) and went for a test drive. The bike was misfiring and had a REAL rough idle but seems OK after a short 5 KM run.
The folowing Thursday morning (one week since being parked)when I went to go to work the bike again had a very rough idle and the bike ran so poorly that I did not take it to work. As we know from the other thread (Timing pickup question) the ignition would appear to be working correctly.
So today is re & re the carbs day to reinstall all the jetting that came with the bike. The jets have been soaking in carb cleaner all night.
While I have the carbs off I will check all rubber seals and blow out all passage ways again.
While I am doing this job I will from time to time take a break and check here for any input that can be offered as to what's going on with this bike.
Rob
The bike had been running reasonably well but seemed to lack pulling power in the mid throttle range and had a misfire at constant throttle settings and a rough misfire idle. Mostly when warming up.
Last Thursday (July 27) I removed the baffle of my MAC 4 into 1 pipe and packed the outside of the baffle to control noise and possible poor exhaust resonance because the stop plate has been removed from the baffle. I used the bike the balance of that day for a few short trips. there was no change to the above condition it was just less noisy.
I parked the bike that Thursday evening to remove and return the front wheel for a defective tire issue.
Got the tire issue issue sorted and reinstalled on Wednesday (Aug 2) and went for a test drive. The bike was misfiring and had a REAL rough idle but seems OK after a short 5 KM run.
The folowing Thursday morning (one week since being parked)when I went to go to work the bike again had a very rough idle and the bike ran so poorly that I did not take it to work. As we know from the other thread (Timing pickup question) the ignition would appear to be working correctly.
So today is re & re the carbs day to reinstall all the jetting that came with the bike. The jets have been soaking in carb cleaner all night.
While I have the carbs off I will check all rubber seals and blow out all passage ways again.
While I am doing this job I will from time to time take a break and check here for any input that can be offered as to what's going on with this bike.
Rob
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