I've enjoyed following the threads of others that bought projects, and kept us posted as they revived them.
Many of you saw my posts here and there as I fixed up a basket case SF that I bought for $400. I finally had it fully ride-able this year, although it needs a few items to make it 'perfectly' maintained.
I decided to start the story of my new purchase, 1980 XS1100SG with full fairing and hard bags.
I brought it home and gave it bath, to remove years of dust. Here it is, except the luggerack/backrest and taillight are removed to fit on my trailer:
I bought it Friday. Good thing I washed it Friday because we got 16" of snow on Saturday! BTW Looks better in the picture than real life.
While it was snowing, I took inventory and went to work. Despite 39k miles, this bike is in much better shape than any of my previous projects.
The only item that is not stock is the fuse panel has been reworked, and while this 'repair' is functionally OK, none of us would be proud of it:
First order of business was to drain the old gas from the tank and the carbs. Too bad the petcocks were left in the ON position. The Octy is there, but apparently has became tired along the way. There are gas stains down the sides of the carburators and all over the top and sides of the engine.
Next I drained nearly 5 quarts of gasoil from the crankcase.
Next I want to know the compression, so off with the fairing:
I don't want to crank too much without oil in the crankcase, but I quickly measured 122/70/118/129; cold with the throttle wide open.
#2 doesn't look happy. I had noticed the plug was loose when I removed it and it had carbon all the way up the threads, indicating it was leaking exhaust. I can see the hole threads look somewhat distorted, I really hope they are not stripped. So far I have put light torque on the threads and they are holding. For now, I'll hope it's not stripped.
So I put a couple of little squirts of oil in the cylinders and got 124/77/124/134. Still troubled by the reading in #2.
So, next I'm gonna remove the carbs, and re-shim the valves.
Then I think I should clean the carbs and put them back on and find out now if I can fix #2 with MMO and exercise. I want to know now if I'm gonna have to pull the head.
So, that's the report so far. Looking for any more thoughts from the community about low compression in #2. I'm secretly hoping that was the one with open exhaust valve while it sat for years, and maybe it rusted a little.
PS: We have spark! Never bought a project that already had spark.
Many of you saw my posts here and there as I fixed up a basket case SF that I bought for $400. I finally had it fully ride-able this year, although it needs a few items to make it 'perfectly' maintained.
I decided to start the story of my new purchase, 1980 XS1100SG with full fairing and hard bags.
I brought it home and gave it bath, to remove years of dust. Here it is, except the luggerack/backrest and taillight are removed to fit on my trailer:
I bought it Friday. Good thing I washed it Friday because we got 16" of snow on Saturday! BTW Looks better in the picture than real life.
While it was snowing, I took inventory and went to work. Despite 39k miles, this bike is in much better shape than any of my previous projects.
The only item that is not stock is the fuse panel has been reworked, and while this 'repair' is functionally OK, none of us would be proud of it:
First order of business was to drain the old gas from the tank and the carbs. Too bad the petcocks were left in the ON position. The Octy is there, but apparently has became tired along the way. There are gas stains down the sides of the carburators and all over the top and sides of the engine.
Next I drained nearly 5 quarts of gasoil from the crankcase.
Next I want to know the compression, so off with the fairing:
I don't want to crank too much without oil in the crankcase, but I quickly measured 122/70/118/129; cold with the throttle wide open.
#2 doesn't look happy. I had noticed the plug was loose when I removed it and it had carbon all the way up the threads, indicating it was leaking exhaust. I can see the hole threads look somewhat distorted, I really hope they are not stripped. So far I have put light torque on the threads and they are holding. For now, I'll hope it's not stripped.
So I put a couple of little squirts of oil in the cylinders and got 124/77/124/134. Still troubled by the reading in #2.
So, next I'm gonna remove the carbs, and re-shim the valves.
Then I think I should clean the carbs and put them back on and find out now if I can fix #2 with MMO and exercise. I want to know now if I'm gonna have to pull the head.
So, that's the report so far. Looking for any more thoughts from the community about low compression in #2. I'm secretly hoping that was the one with open exhaust valve while it sat for years, and maybe it rusted a little.
PS: We have spark! Never bought a project that already had spark.
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