The wrong pilots would certainly cause an issue like this. And, a chugging affect at cruise. BTDT
Are they genuine Mikuni?
Altitude may have an effect also, less air, more gas but the CV carbs are supposed to self adjust for that.
If all else fails, drop the float level 1mm and see if that makes a difference
Are they genuine Mikuni?
Altitude may have an effect also, less air, more gas but the CV carbs are supposed to self adjust for that.
If all else fails, drop the float level 1mm and see if that makes a difference


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......but, least got 2 now known to be good extra TCI's
. Backed out the 2 1/2 settings to highest in.vac. which ended up at 4 turns out. Smoothed out and wasn't laboring with that slight lope, and idle came up. Re-set it back down, rechecked the mix setting, then synced the four. Got an afternoon shower(reprieve finially), so soon as some of the wet dissapears, going for a test run. Report back later as to the results
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