Not to be an over detailed AH, but heck that is me. There is about no possible way that the frame got bent and other items did not get changed out, at least the forks or the swing arm or something.
Yaeh I know, nitpicky AH.
Yaeh I know, nitpicky AH.
I had put penetrating oil down the plug holes, and drained the oil and repaced with new. let it sit 3 days. Hooked up jumper cables and it turned over. Just to see what would happen I re-installed the plugs, sprayed a little starting fluid at the carbs and hit the button. It Fired! Bad news is that I tried to run it and the carbs are totally gummed up. I pulled them down to soak (the diaphragms look great!). Thats when I noticed that the #4 carb pilot jet head was totally stripped out. The jet looks buggered good in the inlet hole, and I know that its clogged with varnish. Should I try heat and an easy out? Should I just soak it and use compressed air? Should I look for another carb to use the body?
If they do not come out fairly easy, then I would hit it with heat, then more penetrating oil and repeat a few times. Heat till the oil smokes off (but do not add heat until the solvents dissolve so you don't need a fire extinguisher). Typically this will get them out.
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