K&L carb controversy renewed...
Well I looked for leaks and check my synch today when I got home.
Synch was off by just a touch between the two banks. Just thinking about turning the adjust screw was almost enough to bring it back.
No vacuum leaks found.
Still fell flat with any kind of throttle input.
Decided to remove the carbs yet again and go through the idle circuits with a fine tooth comb. Compared old parts to new again and found this:
Click here for the full size
The jet on the right is the new K&L idle jet, the jet on the left is the original idle jet. Now I can clearly see that the hole in the original jet is larger then the new jet. Both are stamped 42.5. I can only assume that the K&L jets are not right. I've ordered a set of genuine Mikuni jets and I'll see if that fixes the off idle problems, but they won't be in until Thursday. I really suspect now that my problems have been caused by a way to lean condition because the K&L jets are so much smaller then the Mikuni ones.
Randy:
I suspected that I might need larger mains and I in fact have a set of 140 mains. I tried the 140's and they really stole my mid range but that was with the leaky old emulsion tubes. I intend to try them again with the new tubes once I get the bike ridable. As it is now I consider it un-ridable because taking off is so slow and difficult. You also have the free-er flowing air filter where mine is stock.
Well I looked for leaks and check my synch today when I got home.
Synch was off by just a touch between the two banks. Just thinking about turning the adjust screw was almost enough to bring it back.
No vacuum leaks found.
Still fell flat with any kind of throttle input.
Decided to remove the carbs yet again and go through the idle circuits with a fine tooth comb. Compared old parts to new again and found this:
Click here for the full size
The jet on the right is the new K&L idle jet, the jet on the left is the original idle jet. Now I can clearly see that the hole in the original jet is larger then the new jet. Both are stamped 42.5. I can only assume that the K&L jets are not right. I've ordered a set of genuine Mikuni jets and I'll see if that fixes the off idle problems, but they won't be in until Thursday. I really suspect now that my problems have been caused by a way to lean condition because the K&L jets are so much smaller then the Mikuni ones.
Randy:
I suspected that I might need larger mains and I in fact have a set of 140 mains. I tried the 140's and they really stole my mid range but that was with the leaky old emulsion tubes. I intend to try them again with the new tubes once I get the bike ridable. As it is now I consider it un-ridable because taking off is so slow and difficult. You also have the free-er flowing air filter where mine is stock.
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